欢迎登录材料期刊网

材料期刊网

高级检索

地下管线服役期内发生穿孔失效将会造成严重的安全事故及巨大的经济损失。某厂 X60钢管线埋地一年后,7.1 mm 厚的管身出现蚀孔漏气现象。通过现场调研及 SEM、XRD 取样分析,研究了管壁穿孔失效的腐蚀机制。结果表明:蚀孔全部呈直线状分布于管底,蚀孔附近的腐蚀产物表面含有大量硫、氯元素;EDS 及 XRD 分析确认腐蚀产物为硫铁化合物;钢管内壁基体侧氧化铁皮中含有大量 FeO(OH)腐蚀产物。综合现场腐蚀环境、腐蚀形貌及腐蚀产物的详细分析,明确了蚀孔产生的原因为硫酸盐还原菌造成的微生物腐蚀,结合腐蚀特点及现场情况提出了改进措施。

Pitting in the body of underground pipelines and the failure during their service period will result in serious security incidents and huge economic loss.There appeared pitting in the body of X60 pipeline with the thickness of 7.1mm after 13 months of service,which resulted in air leakage.The corrosion mechanism of the pipeline body pitting was researched through site investigation and sample analysis by SEM and XRD.The results showed that all corrosion holes were located in the bottom of the pipeline in a straight line shape,plenty of S and Cl elements were found in the corrosion product around the holes,which was confirmed as FexSy through EDS and XRD analyses.A plenty of FeO(OH)were found in the scales beside the pipeline body.The cause of the corrosion holes was confirmed with the combination analyses of site environment,corrosion morphology and corrosion products to be microbiological corrosion due to SRB.Improvement measures were proposed according to the corrosion characteristic and site condition.

参考文献

[1] 何攀,刘才学,王瑶,艾琼,宋健.压力管道裂纹泄漏定量技术研究[J].核动力工程,2012(05):32-35.
[2] 宋光雄,张晓庆,常彦衍,张峥,钟群鹏.压力设备腐蚀失效案例统计分析[J].材料工程,2004(02):6-9.
[3] 贾恒磊,赵春平,汪浩,姜姝,费雪松.管线的氧浓差电池现象[J].管道技术与设备,2012(03):51-52.
[4] 王明义,梁小兵,郑娅萍,赵由之,魏中青.硫酸盐还原菌鉴定和检测方法的研究进展[J].微生物学杂志,2005(06):81-84.
[5] 张小里,陈志昕,刘海洪,郭生武,陈开勋.环境因素对硫酸盐还原菌生长的影响[J].中国腐蚀与防护学报,2000(04):224-229.
[6] 谢日彬,李锋,于亮,向安,万钢.硫酸盐还原菌对油田的腐蚀状况及其微生物防控机理[J].山东化工,2011(07):30-33.
上一张 下一张
上一张 下一张
计量
  • 下载量()
  • 访问量()
文章评分
  • 您的评分:
  • 1
    0%
  • 2
    0%
  • 3
    0%
  • 4
    0%
  • 5
    0%